Investigation of Harmonic Losses To Reduce Rotor Copper Loss in Induction Motors for Traction Applications

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Date

2025

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Volume Title

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Multidisciplinary Digital Publishing Institute (MDPI)

Open Access Color

GOLD

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No

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Abstract

The focus of this paper is to seek means of increasing induction motor efficiency to a comparable level to a permanent magnet motor. Harmonic and high-frequency losses increase the rotor core and copper loss, often limiting IM efficiency. The research in this study focuses on reducing rotor core and copper losses for this purpose. An accurate finite element model of a prototype motor is developed. The accuracy of this model in predicting the performance and losses of the prototype motor is verified with experiments over a 32 Hz–125 Hz supply frequency range. The verified model of the motor is used to identify the causes of the rotor core and copper losses of the motor. It is found that the air gap flux density of the motor contains many harmonics, and the slot harmonics are dominant. The distribution of the core loss and the copper loss is investigated on the rotor side. It is discovered that up to 35% of the rotor copper losses and 90% rotor core losses occur in the regions up to 4 mm from the airgap where the harmonics penetrate. To reduce these losses, one solution is to reduce the magnitude of the air gap flux density harmonics. For this purpose, placing a sleeve to cover the slot openings is investigated. The FEA indicates that this measure reduces the harmonic magnitudes and reduces the core and bar losses. However, its effect on efficiency is observed to be limited. This is attributed to the penetration depth of flux density harmonics inside the rotor conductors. To remedy this problem, several FEA-based modifications to the rotor slot shape are investigated to place rotor bars deeper than the harmonic penetration. It is found that placing the bars further away from the rotor surface is very effective. Using a 1 mm sleeve across the stator’s open slots combined with a rotor tapered slot lip positions the bars slightly deeper than the major harmonic penetration depth, making it the optimal solution. This reduces the bar loss by 70% and increases the motor efficiency by 1%. Similar loss reduction is observed over the tested supply frequency range. © 2025 by the authors.

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Keywords

Harmonic Loss Reduction, High-Efficiency Induction Motor, Rotor Copper Loss Reduction, Stray Load Loss Minimization, Surface Loss Reduction, Traction Motor, Transportation engineering, traction motor, TA1001-1280, stray load loss minimization, harmonic loss reduction, Electrical engineering. Electronics. Nuclear engineering, surface loss reduction, high-efficiency induction motor, rotor copper loss reduction, TK1-9971

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WoS Q

Q2

Scopus Q

Q2
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OpenCitations Citation Count
1

Source

World Electric Vehicle Journal

Volume

16

Issue

5

Start Page

248

End Page

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Scopus : 2

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Mendeley Readers : 3

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