Experimental and numerical results of a flapping wing four bar mechanism

dc.authorscopusid55888184200
dc.authorscopusid24438001000
dc.authorscopusid15837320400
dc.contributor.authorArıkan, Kutluk Bilge
dc.contributor.authorArikan,K.B.
dc.contributor.authorKurtulus,D.F.
dc.contributor.otherDepartment of Mechatronics Engineering
dc.date.accessioned2024-07-05T15:44:53Z
dc.date.available2024-07-05T15:44:53Z
dc.date.issued2017
dc.departmentAtılım Universityen_US
dc.department-tempSenol M.G., Department of Aerospace Engineering, Middle East Technical University, Aerospace Engineering Department, Ankara, 06800, Turkey; Arikan K.B., Department of Mechatronic Engineering, Mechatronic Engineering, Atilim University, Ankara, 06836, Turkey; Kurtulus D.F., Department of Aerospace Engineering, Middle East Technical University, Aerospace Engineering Department, Ankara, 06800, Turkeyen_US
dc.description.abstractThis paper explores the design and testing of a flapping wing four-bar mechanism. A four-bar linkage system kinematic analysis is introduced for flapping wing motion. Four-bar mechanism is activated by a servo motor which is driven by microcontroller. The wing undergoes a pure flapping motion at a fixed pitch angle. Force measurements are performed for hover mode by using a force transducer. In addition, 3D numerical analyses are performed and the results are compared with the experimental measurements. Overall, CFD results show good agreement with the experimental data. © 2017 by the American Institute of Aeronautics and Astronautics, Inc. All rights reserved.en_US
dc.identifier.citation1
dc.identifier.doi10.2514/6.2017-0498
dc.identifier.isbn978-162410447-3
dc.identifier.scopus2-s2.0-85017281907
dc.identifier.urihttps://doi.org/10.2514/6.2017-0498
dc.identifier.urihttps://hdl.handle.net/20.500.14411/3839
dc.language.isoenen_US
dc.publisherAmerican Institute of Aeronautics and Astronautics Inc.en_US
dc.relation.ispartofAIAA SciTech Forum - 55th AIAA Aerospace Sciences Meeting -- 55th AIAA Aerospace Sciences Meeting -- 9 January 2017 through 13 January 2017 -- Grapevine -- 126423en_US
dc.relation.publicationcategoryKonferans Öğesi - Uluslararası - Kurum Öğretim Elemanıen_US
dc.rightsinfo:eu-repo/semantics/closedAccessen_US
dc.subject[No Keyword Available]en_US
dc.titleExperimental and numerical results of a flapping wing four bar mechanismen_US
dc.typeConference Objecten_US
dspace.entity.typePublication
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relation.isAuthorOfPublication.latestForDiscovery03706570-0173-42fb-a940-17a9fbbef4b3
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relation.isOrgUnitOfPublication.latestForDiscoverye2a6d0b1-378e-4532-82b1-d17cabc56744

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